[C320-list] Dropping Rudder
Stord at aol.com
Stord at aol.com
Sat Apr 8 12:48:43 PDT 2006
To All,
It was an interesting last week. I found a little play in my cutlass
bearing while the boat was hauled for painting. It was rock solid horizontal, but
had a little play vertical. If all you do is pull sideways on the shaft to
see if it or the strut move, you won't feel the vertical play.
I've got a Martec three bladed feathering prop installed and didn't want to
drill out the locking pin holding the locking nut to the shaft. I was also
at a DIY marina and they didn't have the tool needed to push out the bearing
with the shaft still installed, so I needed to get the shaft out to replace
the bearing.
I had never dropped a rudder before, so the first step was to look at the
Edson steering system. It's fairly simple and comes apart in two large pieces.
I then looked at the rudder to see how it was held in place. There is one
large bolt at he top of the shaft where the emergency tiller goes that holds
it in place. Since it all looked fairly simple, I started.
The next step was digging a hole to drop the rudder. I estimated 24 to 26
inches to get the clearance on the rudder shaft. Unfortunately, I ran into a
large rock at 24 inches that I couldn't get out. I dropped the rudder hoping
it would clear the bottom of the boat. It didn't. The marina offered to
lift the boat another 6 to 8 inched "for a small fee." Since the rudder was
down, but couldn't be moved out, I accepted. He lifted the boat approximately
8 to 12 inches and I had plenty of clearance. He reblocked me at that
height, so I would have the clearance to get the rudder back in. In the future I
will plan on 30 inches minimum to get the rudder shaft clear, if I need to do
it again. Also plan on a couple of helpers to lower and raise the rudder,
while you're in the cockpit working the bolt at the top of the rudder shaft.
The couplings on the shaft at the transmission game apart easily enough when
the bolts were removed, but the coupling on the shaft was stuck even after
the shaft pin was tapped out. After liberal use of WD-40 and some
encouragement from my hammer, the coupling slowly slid of the shaft. I had previously
sanded the shaft to remove all of the "growth" that had built up, so it slid
out of the strut fairly easily. Did I say the yard didn't have a bearing
puller? This is really a DIY yard. In any case, after talking to a Catalina
mechanic at a Catalina facility, I used a large socket from my ratchet set and
my hammer to tap the old bearing out. Of course, it went a little faster once
I loosened the two allen screws in the side of the strut.
While waiting for the new bearing to arrive, I took fine sand paper and
sanded the inside of the strut, the coupling and the end of the shaft. With a
little WD-40, the new bearing went in easily. The shaft went back in. I was
concerned about getting the coupling back on the end of the shaft since it had
been difficult to get off. Again, WD-40 and my hammer did the job. The
slot for the locking pin wasn't perfectly lined up, so I put one of the bolts in
the coupling and tapped it sideways until the slot lined up. Even with
WD-40, it took a little encouragement to get the pin in the slot. I then lined
up the couplings and tightened them.
The rudder went back in easily enough, but the tolerance on the bolt at the
top of the shaft was very tight and it took a little work to get it in. It
was like the bushings on the rudder had expanded just enough to make it
difficult. Once the rudder was in, putting the Edson steering quadrant back
together was relatively easy. The hardest part about that process was the lack of
room to see and move in back there.
We finished painting the boat and splashed it two days later. On motoring
back to our marina, there was a significant vibration from the motor/shaft. I
know the tolerances are tight on the shaft/transmission couplings and I felt
I had been careful with them. Nevertheless, something wasn't right. I know
that boats on blocks don't necessarily have the same shape as they do when
they're in the water and I hoped that might be the problem. We got to our
marina, tied up and called it a day. I went to the boat the next day and
disconnected the shaft/transmission couplings. I ran the motor with the shaft
disconnected to get a baseline vibration. The motor itself had some vibration.
I then slid the two couplings together and slowly rotated the shaft while
keeping the transmission coupling still. I could not see or feel (with a gap
feeler) any gaps. I then tightened the bolts on the couplings 1/4 turn each
while rotating the shaft until they were all equally tight.
We took the boat out today and the excess vibration is gone. I think the
problem was caused by the boat flexing a little on the blocks and my tightening
the shaft at that time. In any case, it was a project that I hadn't
anticipated, but I'm glad I did. I'm a lot more familiar with some of the major
components of the boat and would be comfortable doing maintenance on either one
of them again. My only regret is that I didn't take my camera so I could
post pictures of the process on the web site.
Fair Winds,
Steve Lunsford
s/v Joy 756
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